Friday, September 15, 2023

Airfest 29 Launch - September 1st - 4th, Argonia, KS

 Flight #1: Loc Big Nuke on a AT K805G.   

Launch was straight up, good boost no issues.  Dual deploy worked perfectly and the rocket landed in the beans just north of the field.  Tracker worked perfectly too.





Flight #2:  3x Goblin on an AT I357 motor. Expected altitude was 2400 feet.  Launch and recovery with Chute release worked great. Altus-Metrum Tracker led me directly to the rocket which was in the beans again.

https://youtu.be/C3HF-F4M16A?t=503

Flight #3: 3" Punisher on a AT K805G.    Boosted to 10,662 feet and Mach 1.3. Landed about 1 mile west of the launch site.  Tracker worked perfectly again.


Flight #4: Loc Big Nuke on a AT K700.

Launch was good - slight tilt into the wind, Recovery system worked perfectly. Recovered about 400 meters from the launch site.  Apogee of 5400 feet.  Could see the rocket the entire flight.












Sunday, July 23, 2023

Notra Club Launch Flight Log

 July 22, 2023


Conditions: Nice weather and low wind in the morning, with the wind picking up later in the afternoon.

Flight 1:  Loc Wolverine on an Aerotech I211 with a 10 second delay for motor ejection.  Expected altitude of 2000 feet.  Jolly Logic chute release set for 500 feet.  On board video recorded with a Mobius maxi camera.  Altus Metrum Tracker onboard as well though it was not needed as the rocket landed in the launch field.  

Boost and recovery were good.




Flight 2: Scratch Built 4" Goblin on a CTI I170 with a 10 second delay for motor ejection.  Jolly Logic Chute release set for 500 feet.

Boost and recover were good though it looked like the chute release was a little late in opening.




Sunday, July 9, 2023

LDRS-41 Flight Log

LDRS-41 took place at Richard Bong State Recreation area in southern Wisconsin. July 6-9, 2023

My flights went as follows:

Day 1  - Winds were out of the north 5-10 - which is unfavorable because rockets get pushed into the tree line.  Strategy was to launch low altitude and see how it goes as this was our first time at Bong.

Flight 1:  Rocket R&D Brutus on an I-161 WL motor. This motor was built using cut and cored grains procured from RCS.  Estimated Altitude was 2000 feet, no altimeter was on board.  Flight was good and landing was lucky as it just missed landing in a small pond just east of the flight line (near the away cell).



Day 2 - Better winds, nice weather, 75 F and sunny most of the day. High clouds rolled in around noon.

Flight 2: Loc Big Nuke on a K550. The motor was built using cut and cored 54mm white lightning grains.

Dual deploy with Altus Metrum Easy Mini as primary altimeter, and Eggtimer Classic as backup altimeter.

Launch was good but the rocket veered to the south just after leaving the 15-15 rail (which was too short at 6 feet).  Recorded apogee of 3821 feet, with a maximum speed of 515 fps (mach 0.5). Drogue descent rate was 51 fps, and main chute descent rate was 19 fps.  The eggtimer classic functioned correctly in providing the backup charges,



The Altus Metrum TeleGPS was utilized for tracking and it worked flawlessly, leading me directly to the rocket which was located in tall grass and shrubs near the tree line to the south of the flight line.

Day 3  - Started with rain lasting until about 10:00 am and then a low cloud deck until about 11:30.  Then became partly cloudy and warm

Flight 3: Punisher 3 on an I284 (cut and cored RCS grains). Launch was good but the rocket veered north shortly after leaving the pad.  The reason for this is unclear as the rocket was at least 6 feet above the rail before turning, and the wind was low. This rocket had flown perfectly straight on a blue thunder motor at the previous launch.

Possible causes:

1. Nozzle was not drilled straight causing a slight thrust vector. (I hand drilled the nozzle for this motor).

2. Debris from the burning propellant clogged a section of the nozzle.  Maybe the grain core was "shaggy" and not smooth allowing for more debris.  I have to wonder if white lightning propellent is more prone to produce slag that could clog the nozzle.

The eggtimer quantum recorded an altitude of 2955 feet.  Once again the TeleGPS provided the guidance to easily locate the rocket north of the park access road on the north side of the launch field. Recorded max velocity was 453 fps, drogue descent @ 55 fps and main descent rate was 16 fps.




Chip's Flight log
Day 1 - Unfamiliarity with the site was cause for apprehension. Experienced members gave insight as to what to expect. With the winds blowing in the atypical North to South, caution was the approach. I was not alone as others seemed to hold back until we could get a hint as to what the results would be. Seemed like a safe bet to send up the 3" Cherokee on an H128 with the JLCR.. The H-128 was the last commercial motor for that case I believe. The launch was typical for the Cherokee, straight and true. Without an altimeter, Open Rocket calculated a flight of 970’ AGL. Did not have a sim at the time so I guessed at the 6 second delay, which was very close to perfect. The RunCam shut off on the pad therefore no launch video.





Day 2.  - Trying to get the recovery monkey off my back with the Cherokee 3XE. Added a Stratologger altimeter to the existing RRC2 for redundancy. This would be the fourth launch on this and it had yet to come down under full parachute! Careful preparation and packing of the recovery system resulted in the first main parachute recovery. The liftoff on an I-211 reload (Which I believe was an EMK with 38mm cut grains lifted it to 1352' AGL and FINALLY produced a main chute recovery. Drogue and main chute both functioned properly. The main parachute was a homemade 50” black and yellow ripstop nylon chute. The descent rate was good, although I need to buy the cable to download the data from the Stratologger. All charges fired! The recovery was not flawless as the location of the drogue caused the two harnesses to become entangled. The seems to be an ongoing issues with the owner. On the plus side, Mom had previously sewn a deployment bag for this one, out of yellow Nomex fabric, that can be seen in the recovery pic. Randy snapped a recovery pic also known as “evidence.” Once again, the Runcam failed to get video which means that it has flown its last flight.



 




Day 3. Time today was cut short by the miserable early weather.



Finally getting to the 5.5” Slugbuster!






More careful preparation ensued as the two altimeters were set up with charges. The Eggtimer Proton taking the lead and the Eggtimer Classic (under new programming) would handle the cleanup. No more relying on single altimeters for me. Also joining the electronic party, the altimeters would be accompanied by an Altus Metrum GPS tracker, for the first time. The rocket was loaded with a 54mm J-415 EMK 54-1280 with cut grains. That rocket shot off the pad to an altitude of 2842' and both altimeters functioned perfectly.




A very nice flight, straight and true. The dual recovery worked well EXCEPT it almost became entangled - I really need to change the location of the drogue! The descent rate was nearly 30 feet/second so this bird is going to receive new laundry in the form of twin 60” diameter chutes..It went off into the field to the south and the tracker proved its worth. It led us to the recovery location without a hitch.




























Wednesday, June 14, 2023

URRF 9 flight Log - Potter New York

My Flights -  

Friday June 9th, 2023

Launch #1

Wildman Punisher (3 inch diameter) first flight on an Aerotech I357 Blue Thunder EX built motor - I cut and drilled the grains and the delay element and assembled the motor using an EMK360 kit. 

The altimeter was an Eggtimer Quantum configured for auto-arm, and mains deployment at 500 feet.

Three m2 shear pins were installed on the nose cone. No shear pins were used on the airframe.

The rocket was setup with a main black powder charge of 1.8g, and an apogee charge of  1.5g  

Boost was perfect with a recoded apogee of  1923 feet.  Apogee charge fired as expected at 1911 feet.

Descent rate on the drogue was 60 ft/second and  then the main charge fired at about 411 feet with a descent rate on the main chute of 22 feet/second.

No tracker onboard and rocket was visible through the boost and recovery phases.



Saturday June 10th, 2023

Launch #1

Loc Wolverine on a CTI J354 configured for 12 second delay. Estimated Altitude was 3780 feet using open rocket.

Rocket had a runcam 2 4k onboard and a jolly logic chute release set for 600 feet.

Boost was good, deployment occurred at apogee. Chute release performed as expected.  

Rocket was visible through the entire boost and recovery phase.

Included a eggfinder mini GPS tracker and used my new Eggfinder LCD receiver as well as the Eggfinder BT receiver. Neither worked correctly, all indicated the completely wrong direction to recover the rocket.


Launch #2

First flight of the Loc Big Nuke 3E (Children of Atom edition) on a Aerotech J415.   RSO weighed the rocket at 14 lbs and 15 oz - which is much heavier than the simulation weight.

Simulated altitude was 3600 feet but the actual recorded altitude was 2780 feet (848 m).

The rocket was configured with a Eggtimer classic as the primary flight controller, and an  Altus Metrum easy-mini as the backup flight controller. 

I incorrectly configured the Eggtimer classic so while it did record the flight data, it did not fire any recovery charges.

I also incorrectly configured the Easy-mini - I thought I set the main charge altitude to 500 feet but I actually set it to 500 meters. The mains were deployed at a high altitude and it was windy so I had to walk a couple of miles to retrieve the rocket.








Sunday June 11th, 2023

Loc Wolverine on a CTI J335 Red with an estimated altitude of 3300 feet.  Chute release was set to 600 feet but for some reason the main chute came out at apogee.  Winds were low so this had minimal effect on the recovery.




===============================================================

Chip's Flights -


URRF 2023 - Potter NY - June 9-11


Friday June 9


Peacock - F37 6 sec delay was perfect.  Open rocket called for 4 sec.

Parachute did not hang up inside this time.

 

LOC Stovi H128 HEADS UP!  That thing was gone quickly.  Need better glasses. Good recovery.  Finally saw it coming down when it was nearly all the way down.



Saturday June 10


Bull Pup - I245G-10 Jollylogic Chute Release at 500’ Boost and recovery, did not see it for most of the flight.


Cherokee 3XE - J330 - RRC2+ set to 500’ - No main Again! No altitude reported.  Drogue charge fired, main charge did not, chute did not deploy.  Nose cone was off but not due to black powder charge.  Chute could not pull itself from the deployment bag - far too tight. Recovery harnesses were a tangled mess!  Upon inspection, discovered that wires on altimeter were loose. Failure likely due to power interruption during flight.  Altimeter later tested with LED’s and Shop Vac and found to be functional.  Going to add another altimeter and go again. Used 2 grams on drogue and 2.5 on main.


Sunday June 11


Slugbuster - J330 motor - reached an altitude of 1644’. Without sufficient eyewear, no sense in sending this higher than 2000 ft. At least I saw it for the entire duration. Open Rocket simmed to just over 2000’ - need to double check the weight. 




Wednesday, June 15, 2022

Ohio Storm Damage June 13th, 2022

 On June 13th a terrible storm hit southern Wayne county in Ohio.   Below are some images of some of the damage.


Drone footage of the downed trees


Smyser Road is closed



Pile of fallen trees


Trees Snapped off


Monday, June 28, 2021

Another 4K Rocket Launch Video

The Brutus again - this time on an Aerotech I285 Redline motor. The motor took too long to light and therefore the ejection charge was too early. (Seems to be an ongoing issue with the redline motors). 

The rocket was not damaged.



Sunday, June 6, 2021

Mid Ohio Rocket Launch photos

Don't know whose rocket but I like the photo.




 My Loc-Precision Wolverine on an I366 motor that fired late and therefore the delay burned through and the ejection charge fired early causing a massive tear in the airframe.   Everything looks good here though.